Previous Page  41 / 52 Next Page
Information
Show Menu
Previous Page 41 / 52 Next Page
Page Background

This was 5 725 tons less than the average 197 453 tons of air per month

consumed before the ring was split. This saving is a combination of

the air saved as a result of a reduced line pressure leading to smaller

line friction losses as well as the reduced amount of air lost through

air leaks.

Figure 8

shows the pressure profile of the low pressure side

after the control valves were installed and commissioned.

Figure 8: Low pressure at the plants.

The reduced energy consumption, which can be calculated from the

area under the actual power profile of

Figure 9

, is clearly evident.

This saving was achieved through a reduction in pressure on the low

pressure side of 80 kPa.

Figure 9

shows the actual average power

consumption, after project implementation, over a period of one

month, against the original power baseline before the project was

implemented. The average daily energy efficiency saving achieved

was 43,2 MWh.

Figure 9: Actual power profile vs. baseline.

Conclusion

Evaluation of the compressed air system at a gold mine showed that

it is possible to reduce the pressure and air flow in certain sections

of the mine. This was accomplished by installing automatic pressure

reducing control valves in the compressed air delivery line. When

these valves are signalled to reduce the downstream pressure, they

cause the upstream pressure to increase. The increased upstream

pressure will cause the compressors to reduce their output to stay

take note

Rudi Joubert, HPR, is a registered professional engineer.

He holds a Masters degree in electrical engineering and

is enrolled for PhD studies at North-West University.

E-mail:

rjoubert@researchtoolbox.com

Dr Johann van Rensburg is a registered professional

engineer and holds a PhD in electrical engineering from

the North-West University. He is a senior lecturer at the

North-West University.

E-mail:

10728023@nwu.ac.za

Dr Ruaan Pelzer holds a PhD in mechanical engineering

from the North-West University. He is a senior lecturer at

the North-West University.

Email:

rpelzer@rems2.com

ENERGY + ENVIROFICIENCY:

FOCUS ON VALVES + ACTUATORS

within the output pressure set point range. The reduced output means

less power is required and this will result in significant electrical

energy savings. This saving can clearly be seen in the results of the

case study.

References

[1] Hughes A, Howells MI, Trikam A, Kenny AR, van Es D. A study of

demand side management potential in South African industries.

Energize. Sept. 2006.

[2] Mott RL. Applied fluid mechanics, 6

th

ed. Upper Saddle River.

Pearson Education Inc. 2006.

[3] Zucker RD. Gas Dynamics, 2

nd

ed. Hoboken. John Wiley & Sons.

2002.

[4] Plint MA, Boswirth L. Fluid mechanics: A laboratory course,

London. Charles Griffin & Company Ltd. 1978.

[5] Cerci Y, Cengel YA, Turner HT. Reducing the cost of compressed

air in industrial facilities. Thermodynamics and the Design, Analy-

sis and Improvement of Energy Systems.

Plant pressure

Time in hour

Low pressure side

500.00

450.00

400.00

350.00

300.00

250.00

200.00

150.00

100.00

50.00

0.00

1 2 3 4 5 6 7 8 9 10 11 12 13 14 15 16 17 18 19 20 21 22 23 24

Pressure in kPa

Actual

consumption

Baseline

Time in hours

45000.00

40000.00

35000.00

30000.00

25000.00

20000.00

15000.00

10000.00

5000.00

0.00

Power in kW

1 2 3 4 5 6 7 8 9 10 11 12 13 14 15 16 17 18 19 20 21 22 23 24

• Energy, like water, should be seen as a resource to be

nurtured.

• Every opportunity to improve energy efficiency must be taken.

• Compressed air systems use large amounts of energy and

are prime targets for improved efficiency.

39

February ‘16

Electricity+Control